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 Post subject: sick /6 motor
PostPosted: Tue Oct 02, 2018 6:14 pm 
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4 BBL ''Hyper-Pak''

Joined: Wed Aug 29, 2018 11:44 am
Posts: 31
Location: Payson, Az
Car Model: 1974 Plymouth Duster
After getting some horrendous results on my leak down test, I finally pulled the head off my 225 /6 motor. As I suspected, blown head gasket in #4 hole. Also the valves seats were in really bad shape. Whom ever did the last valve job, didn't know what they were doing, as the valve seats were all over the place - some sunk, some seats almost off the valve face, some valves with almost no margin left on them. Heads gonna need new seats, valves, springs, and guides. On the plus side, no grooving on the block from the blown gasket. Gonna pull .090" off the head surface and bolt it back on. Might do some minor bowl porting. Cylinder bores are stock and the taper measures in the .015 to .022" range.


Attachments:
blownhead gasket4.jpg
blownhead gasket4.jpg [ 232.02 KiB | Viewed 7248 times ]
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 Post subject: Re: sick /6 motor
PostPosted: Tue Oct 02, 2018 10:58 pm 
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Joined: Thu Oct 17, 2002 7:27 pm
Posts: 14769
Location: Park Forest, Illinoisy
Car Model: 68 Valiant
Now would be a great time to just grind the seats out and put in bigger valves John. :mrgreen:

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 Post subject: Re: sick /6 motor
PostPosted: Wed Oct 03, 2018 7:26 am 
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Joined: Mon Oct 21, 2002 11:08 am
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Location: Blacksburg, VA
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You might have had valve recession, so stainless valves would help that. Most of the 1.70/1.44 oversize valves are stainless. I am not sure who is selling them now - SI Valves??

Best,
Lou

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 Post subject: Re: sick /6 motor
PostPosted: Thu Oct 04, 2018 5:19 pm 
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4 BBL ''Hyper-Pak''

Joined: Wed Aug 29, 2018 11:44 am
Posts: 31
Location: Payson, Az
Car Model: 1974 Plymouth Duster
Soooo, Got my head back from my machinist - new stock valves ( back cut @ 25* ), springs, guides, seals and head milled .090". Combustion chambers CC,ed at 48CC's. With stock bore / stroke, .042" compressed gasket thickness, pistons .163" down the hole, I ended up with 8.79:1 CR. I did not run the numbers with stock combustion chambers ( wouldn't hold fluid ), but the CR had to be ridiculously low.


Attachments:
48ccchambers.jpg
48ccchambers.jpg [ 220.18 KiB | Viewed 7172 times ]
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 Post subject: Re: sick /6 motor
PostPosted: Thu Oct 04, 2018 5:29 pm 
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Joined: Thu Oct 17, 2002 7:27 pm
Posts: 14769
Location: Park Forest, Illinoisy
Car Model: 68 Valiant
7.5ish would not be unusual John. Tolerances were very "liberal" from Ma Mopar. :D

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 Post subject: Re: sick /6 motor
PostPosted: Thu Oct 04, 2018 8:29 pm 
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4 BBL ''Hyper-Pak''

Joined: Wed Aug 29, 2018 11:44 am
Posts: 31
Location: Payson, Az
Car Model: 1974 Plymouth Duster
Quote:
7.5ish would not be unusual John. Tolerances were very "liberal" from Ma Mopar. :D
Holly Molly! Factory spec is 8.4:1. :? Well, on the plus side, I should still be able to run "tom cat piss" without a detonation problem. :D


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 Post subject: Re: sick /6 motor
PostPosted: Thu Oct 04, 2018 10:09 pm 
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4 BBL ''Hyper-Pak''

Joined: Sun Aug 12, 2018 1:20 am
Posts: 29
Location: Australia
Car Model: VC valiant regal
Nice work, I'm interested in what you've done because I'm tossing up between just headwork like you fit a budget option..... vs ground up rebuild.
I think I might be surprised by the improvement of just the work you have done to my tired /6.
Thanks for sharing.


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 Post subject: Re: sick /6 motor
PostPosted: Thu Oct 04, 2018 10:13 pm 
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4 BBL ''Hyper-Pak''

Joined: Sun Aug 12, 2018 1:20 am
Posts: 29
Location: Australia
Car Model: VC valiant regal
Quote:
You might have had valve recession, so stainless valves would help that. Most of the 1.70/1.44 oversize valves are stainless. I am not sure who is selling them now - SI Valves??

Best,
Lou
Hey Lou, if those are the oversize valves, the stock ones must be quite small? Silly question, but why would you go oversize? What's the main benefit and what other matching components do you have to have to make it work the best?
Thanks


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 Post subject: Re: sick /6 motor
PostPosted: Fri Oct 05, 2018 4:15 am 
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Joined: Mon Oct 21, 2002 11:08 am
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Location: Blacksburg, VA
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Stock are 1.62/1.36". You should do some bowl porting/blending to take advantage of the bigger valves. Otherwise, they will only help performance at all speeds. I usually mill the head to raise compression to at least 8.5 or 9:1 and (if increasing CR) put in a mild cam like the Howards cam I just posted about.

Lou

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 Post subject: Re: sick /6 motor
PostPosted: Fri Oct 05, 2018 10:24 am 
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4 BBL ''Hyper-Pak''

Joined: Wed Aug 29, 2018 11:44 am
Posts: 31
Location: Payson, Az
Car Model: 1974 Plymouth Duster
Quote:
Nice work, I'm interested in what you've done because I'm tossing up between just headwork like you fit a budget option..... vs ground up rebuild.
I think I might be surprised by the improvement of just the work you have done to my tired /6.
Thanks for sharing.
I forgot to mention that the exhaust valve seats were replaced also, as the recession was just too bad to save them.
I have to continually keep myself in check on this project and stay with my original plan and allotted budget - a nice driver for 12K. Remember, this was a junk yard car.

Bigger valves with 5/32" stems, Port work, all crossed my mind ( not to mention pulling the engine and doing it all ). I think that just getting the head straightened out will put me in the "nice driver" range. Down the road, I might buy a complete used 225 and make it something more than a "nice driver". I have learned over the years to have a plan to start with and stick to it. "Well, if you want to do it the right way " - That comment always equates to more $, and it's easy to say when it aint yo $! I will probably do a little port matching and bolt things back together.

On another note, there is an article in the November issue of Mopar Muscle entitled "Making slat 6 sense". They said that all /6 exhaust manifolds had a 2 1/4" outlet. Not so. Mine measured 2". I will be running a 2" exhaust pipe ( to match the 2" exhaust manifold outlet ) in to a 2 1/2" inlet 2" dual outlet Flowmaster muffler with dual 2" tail pipes. Should be more than adequate for a stock 225. The other part of this article was about updating your point ignition with a new D.U.I. ignition. Beside their HP improvement claims being in the fantasy land range, ( just my opinion and especially if you are already running an electronic ignition system on a stock motor), the D.U.I. ignition does not have a vacuum advance system, which the article claims you do not need with the new D.U.I. ignition. Aint buying that one ether, especially for street operation.


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 Post subject: Re: sick /6 motor
PostPosted: Sun Oct 07, 2018 4:12 am 
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4 BBL ''Hyper-Pak''

Joined: Sun Aug 12, 2018 1:20 am
Posts: 29
Location: Australia
Car Model: VC valiant regal
Quote:
Stock are 1.62/1.36". You should do some bowl porting/blending to take advantage of the bigger valves. Otherwise, they will only help performance at all speeds. I usually mill the head to raise compression to at least 8.5 or 9:1 and (if increasing CR) put in a mild cam like the Howards cam I just posted about.

Lou
Thanks Lou, that's exactly what I'm aiming for. Will this be ok on a bottom end that has not been rebuilt?

And I can't find the specs of the Howard's cam you mentioned? Thanks


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 Post subject: Re: sick /6 motor
PostPosted: Sun Oct 07, 2018 6:06 am 
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Joined: Mon Oct 21, 2002 11:08 am
Posts: 17296
Location: Blacksburg, VA
Car Model:
Assuming your rings are OK, you should be fine. Did you do a compression test, by chance (engine warmed up), before you tore it down?

Here is the link to the Howards cam discussion:

http://slantsix.org/forum/viewtopic.php?f=19&t=62844

The search function is very helpful on this board. If you search "howards" then that thread comes right up.

Lou

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 Post subject: Re: sick /6 motor
PostPosted: Sun Oct 07, 2018 7:12 am 
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4 BBL ''Hyper-Pak''

Joined: Wed Aug 29, 2018 11:44 am
Posts: 31
Location: Payson, Az
Car Model: 1974 Plymouth Duster
Quote:
Assuming your rings are OK, you should be fine. Did you do a compression test, by chance (engine warmed up), before you tore it down?

Here is the link to the Howards cam discussion:

http://slantsix.org/forum/viewtopic.php?f=19&t=62844

The search function is very helpful on this board. If you search "howards" then that thread comes right up.

Lou
Thanks for the link. I'm running a NA motor. Did both a Comp test and leak down test. Both were really bad. Leak down showed most the leak past the valves ( both in & ex). I'm sure it could use rings ( taper measured around .015 to .022 ), but I'm not going there right now.

On another note, check out the attached pics. While looking in to the thermostat housing hole I found two lengths of wire in the water jacket. The one I removed ( laying on the head in one pic) came out of the water jacket on the port side of the comb chambers. The other wire is still in the head ( other pic ) and it is on the lifter side of the chambers. Just started to fish it out in that pic. ????????????????? I have no clue as to how they got in there or why.


Attachments:
wire in head 3.jpg
wire in head 3.jpg [ 252.18 KiB | Viewed 7047 times ]
wire in head 1.jpg
wire in head 1.jpg [ 204.93 KiB | Viewed 7047 times ]
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 Post subject: Re: sick /6 motor
PostPosted: Sun Oct 07, 2018 8:57 am 
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Joined: Mon Mar 31, 2003 1:04 pm
Posts: 7457
Location: Oregon
Car Model: 2023 Eichman Digger?
The wires are part of the casting process. Once casting is complete, the sand is removed, but the wire that holds the sand during the pour remain in place.

CJ

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 Post subject: Re: sick /6 motor
PostPosted: Sun Oct 07, 2018 5:22 pm 
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4 BBL ''Hyper-Pak''

Joined: Sun Aug 12, 2018 1:20 am
Posts: 29
Location: Australia
Car Model: VC valiant regal
Quote:
Soooo, Got my head back from my machinist - new stock valves ( back cut @ 25* ), springs, guides, seals and head milled .090". Combustion chambers CC,ed at 48CC's. With stock bore / stroke, .042" compressed gasket thickness, pistons .163" down the hole, I ended up with 8.79:1 CR. I did not run the numbers with stock combustion chambers ( wouldn't hold fluid ), but the CR had to be ridiculously low.
Thanks for posting up the info - when you milled the head 90 thou, did you need shorter or resized or new pushrods?
Cheers


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